On takeoff I recognized the stall warning horn and an abnormal pitch up after rotation. I immediately provided full forward pressure on the stick and received no response. I proceeded to reduce power and add full forward trim, which lowered the nose of the aircraft. It became clear that the plane did not have elevator control.
First flight out of maintenance goes awry
by General Aviation News Staff | Aug 30, 2022 | #Aircraft, ASRS Reports, Aviation News, Aviation Safety Reporting System, flying, General Aviation, Pilots | 0 comments